christiane
15+ Year Contributor
- 86
- 0
- Jan 20, 2004
-
South Point,
Ohio
I have a new 6 bolt short block in my car. My 6 bolt has less than 200 miles on it and it has smoked since the first time I fired it up. The smoke is minimal to completely absent at idle. The smoke appears to be far worse after a pull (I am only running 4 lbs of boost as part of the engine break in procedure). In what may be a related issue if I drive the car for more than ten minutes it starts to miss terribly to the point that it will barely pull. When it does this I can turn the car off coast and then restart the car and it will be OK for a little while then it goes back to the same thing. The longer the car is off the longer the time between these occurrences.
The turbo does have some play in it. It does not feel as though there is any in and out play, but if the motor is not running there is a fair amount of up and down/ side to side movement.
Here is a summary of what I have done thus far:
First thing I did was perform a compression test below are the results of this rest.
cylinder compression
1 165
2 170
3 168
4 167
*These readings are the most recent after the rings have seated more.
I also performed a leak down test but the new gauge I purchased (Ebay POS) broke; however I was able to listen for air that was escaping the combustion chamber. I did hear some air coming out of the dip stick. Putting my finger over the dipstick diverted the air out of the valve cover to the catch can would be.
Does anyone have any insight they could offer as to the cause of this.
Thanks for the space,
The turbo does have some play in it. It does not feel as though there is any in and out play, but if the motor is not running there is a fair amount of up and down/ side to side movement.
Here is a summary of what I have done thus far:
First thing I did was perform a compression test below are the results of this rest.
cylinder compression
1 165
2 170
3 168
4 167
*These readings are the most recent after the rings have seated more.
I also performed a leak down test but the new gauge I purchased (Ebay POS) broke; however I was able to listen for air that was escaping the combustion chamber. I did hear some air coming out of the dip stick. Putting my finger over the dipstick diverted the air out of the valve cover to the catch can would be.
Does anyone have any insight they could offer as to the cause of this.
Thanks for the space,