12sec92Tsi
15+ Year Contributor
- 187
- 2
- Jul 20, 2004
-
Hagerstown,
Maryland
Well today I decided to check the compression on my motor before spending any more huge amounts of money on upgrades. The results were not good, 140-145-50-150. Awhile back my t-belt jumped 2 or 3 teeth but only ran like that for like 1 minute before I parked it and fixed it the next day. Then I noticed a vibration I did not have before like the bs is out of phase. All the timing marks were lined up. So I'm thinking running it like that for those couple minutes could have bent some valves?? The motor is only like 15-20k miles old since it was completely rebuilt, so the rings should be fine, don't know why they'd be messed up, plus I have a normal 25 psi oil pressure and it's not burning any between oil changes. Another theory I had was the head gasket because I'm only getting like 12 in hg of vacuum at idle and 15 on decel. What do you guys think. Should I just pull the head and replace the head gasket and valves all in one shot and try to fix everything?? I was thinking just pull the head and put on the following things:
Cometic head gasket
ARP head studs
SS oversize valves
Titanium springs and retainers
Also what else should I replace in the valvetrain while in there. Valve guides, seals, etc.?? I'm just really disappointed this happened less than a year since I've had the car on a fresh motor.
Just let me know what you guys think the problem is and what I shoud replace while the head is off. Thanks alot. 
Cometic head gasket
ARP head studs
SS oversize valves
Titanium springs and retainers
Also what else should I replace in the valvetrain while in there. Valve guides, seals, etc.?? I'm just really disappointed this happened less than a year since I've had the car on a fresh motor.
Just let me know what you guys think the problem is and what I shoud replace while the head is off. Thanks alot. 

So I do another test today by myself and zip tied the throttle plate the whole way open while I cranked it and then got out quickly to check the gauge. Boy was I releived with the results, 150 across all four.
So thanks anyways for all you guys advice, and sorry to post about a problem that turns our to be nothing. But it makes me feel much better now that I know I have a good motor to continue to mod.