Intrusive97gsx
20+ Year Contributor
- 95
- 64
- Sep 10, 2002
-
Greensboro,
North Carolina
I went to the track last night and the results weren't even close to what I was expecting. Last week I was pulling 97.75mph in the 1/8 on pump gas and this week I'm only getting around 92mph. For some reason I was only getting around 11 degrees of timing when my AEM map normally pulls to around 19 degrees. It was pulling timing and adding fuel with the around the same amount of knock I normally have and I didn't change anything from last week. Because it was adding fuel I was running around 10.75:1 A/f instead of my usual 11.2:1 A/F, still haven't figured out what happened but I'm working on it.
I figured the EMS was just being a pain in the ass because on one run the car was sputtering the whole way down the track and when I tried to look at my log, it said that the file contained no data. Then I noticed my battery was REALLY low on the laptop so I shut it down and planned on calling it quits
. After I unpluged the laptop I decided I'd give it one my shot... and the car ran fine
(still wasn't running RIGHT, but wasn't sputtering). So here's a look at my messed up pump gas runs.
pump gas
Last night on 21psi
R/T...0.708
60'...1.601
330'...4.812
1/8ET...7.490
1/8MPH...91.93
1000'...9.784
1/4ET...11.734
1/4MPH...116.48
Last week on 21psi
R/T...0.891
60'...1.786
330'...4.937
1/8...7.510
MPH...97.75
Look for better times to come as I plan to fix the problem and return to the track ASAP.
Engine:
BJ 2.3 liter Stroker, 8.5:1 Weisco pistons, Crower rods, ARP hardware
BJ stage 3 cylinderhead, HKS 272/272 Cams
Turbo:
Forced Performance FP-3065
Engine Management:
AEM EMS standalone
Intake:
Forced Performance FMIC, Tial BOV, Accufab 75mm TB
BJ intake manifold
Exhaust:
Tial 40mm Wastegate, FP O2 housing, 3 Downpipe/ testpipe
3 Thermal R&D cat-back
Fuel
Walbro 255hp intank, Walbro 392 inline, Aeromotive AFPR @50psi
880cc Injectors
Drivetrain:
BM Race Tranny, Quaife Center LSD, ACT 2900, Fidanza Flywheel
I figured the EMS was just being a pain in the ass because on one run the car was sputtering the whole way down the track and when I tried to look at my log, it said that the file contained no data. Then I noticed my battery was REALLY low on the laptop so I shut it down and planned on calling it quits
. After I unpluged the laptop I decided I'd give it one my shot... and the car ran fine
(still wasn't running RIGHT, but wasn't sputtering). So here's a look at my messed up pump gas runs.pump gas
Last night on 21psi
R/T...0.708
60'...1.601
330'...4.812
1/8ET...7.490
1/8MPH...91.93
1000'...9.784
1/4ET...11.734
1/4MPH...116.48
Last week on 21psi
R/T...0.891
60'...1.786
330'...4.937
1/8...7.510
MPH...97.75
Look for better times to come as I plan to fix the problem and return to the track ASAP.
Engine:
BJ 2.3 liter Stroker, 8.5:1 Weisco pistons, Crower rods, ARP hardware
BJ stage 3 cylinderhead, HKS 272/272 Cams
Turbo:
Forced Performance FP-3065
Engine Management:
AEM EMS standalone
Intake:
Forced Performance FMIC, Tial BOV, Accufab 75mm TB
BJ intake manifold
Exhaust:
Tial 40mm Wastegate, FP O2 housing, 3 Downpipe/ testpipe
3 Thermal R&D cat-back
Fuel
Walbro 255hp intank, Walbro 392 inline, Aeromotive AFPR @50psi
880cc Injectors
Drivetrain:
BM Race Tranny, Quaife Center LSD, ACT 2900, Fidanza Flywheel
