| Welcome to DSMtuners |
You are currently browsing the site as a "Guest", which means your are either not registered or not logged in. This also means you have limited access to our site and cannot participate - you also are browsing the site with more advertisements than logged-in members.
Register an account and start participating!
|
| Bolt-on Tech: 4G63 intake, exhaust, intake manifold, ignition, fuel system, cooling, etc. |
 |
|
05-25-2012, 03:46 PM
|
Show Printable Version
Email this Post
#1 (permalink)
|
|
Proven Member

From: Levittown, Pennsylvania
Registered: Feb 2012
Reputation:
|
Unbelievable flex pipe failure with pictures
____________________________
97 GS-TALON
|
|
|
|
05-25-2012, 04:01 PM
|
Show Printable Version
Email this Post
#2 (permalink)
|
|
Proven Member

From: Ft.lauderdale, Florida
Registered: Dec 2007
Reputation:
|
Didnt happen to be an Ebay dp? Seen it happen on cars that gotem off Ebay then came to my shop with same problem
|
|
|
05-25-2012, 04:11 PM
|
Show Printable Version
Email this Post
#3 (permalink)
|
|
Supporting Member

From: Nowhere, Wisconsin
Registered: Jan 2008
Reputation:
|
Wow that is kind of crazy.Well more thank kind of.
Umm an ebay Dp should not matter.We did something close to this a week ago.We backed up my talon with only the Dp bolted on.Caught the back of the DP on the cement.And it crimped it.Have not taken it off to look tho yet.But it dis not look like it did a few minutes before that.
____________________________
Turbo by Jusmx141
Tune by My1gdsm
Jedi in training
|
|
|
05-25-2012, 06:09 PM
|
Show Printable Version
Email this Post
#4 (permalink)
|
|
Proven Member

From: Levittown, Pennsylvania
Registered: Feb 2012
Reputation:
|
Not an ebay pipe. It was an exhaust shop generic flex. The guy that replaced it said over the 1000 he has done he has yet to see something like that. My turbo spooled like shit. Now i know why...
____________________________
97 GS-TALON
|
|
|
|
05-25-2012, 06:32 PM
|
Show Printable Version
Email this Post
#5 (permalink)
|
|
Proven Member

From: omaha, Nebraska
Registered: Feb 2005
Reputation:
|
Seen that a few times around here and other forums. Still always pretty amazing to see them fail like that.
|
|
|
|
05-25-2012, 06:32 PM
|
Show Printable Version
Email this Post
#6 (permalink)
|
|
Proven Member

From: New Britain, Connecticut
Registered: Apr 2010
Reputation:
|
Wow that sucker caved in pretty bad.
Well, on the bright side, atleast you cured your car's asthma
|
|
|
|
05-25-2012, 11:59 PM
|
Show Printable Version
Email this Post
#7 (permalink)
|
|
Proven Member

From: Piscataway, New Jersey
Registered: Dec 2006
|
Get a new flex pipe with an interlock liner and you won't have an issue with the flex collapsing.
____________________________
Tim
Grace: 1998 GST
Sera: 1998 XJ
|
|
|
05-26-2012, 03:56 AM
|
Show Printable Version
Email this Post
#8 (permalink)
|
|
Proven Member

From: Levittown, Pennsylvania
Registered: Feb 2012
Reputation:
|
Im thinking that it was caused by my motor mounts. They were bad... REALLY BAD.. The front roll stop fell apart when I took it out and the others weren't much better. The only one that wasnt really cracked and deteriorated was my upper trans mount. That flex pipe was only 3 years old at most but its all better now.
____________________________
97 GS-TALON
|
|
|
|
05-26-2012, 04:09 AM
|
Show Printable Version
Email this Post
#9 (permalink)
|
|
Supporting Freelancer
DSM Revival

From: Roebuck, South Carolina
Registered: Jun 2011
Reputation:
|
Jeez that's crazy. Is there no liner to the flex wire? My flex pipe broke but it had and accordian like inner pipe that the flex wire wrapped around
____________________________
Turbo rebuilder/engine BUilder-rebuilder/5spd rebuilder-builder
90 day warranties.
|
|
|
05-26-2012, 06:01 AM
|
Show Printable Version
Email this Post
#10 (permalink)
|
|
Proven Member

From: Levittown, Pennsylvania
Registered: Feb 2012
Reputation:
|
Yeah theres the inner braid that collapsed and then the hard "accordian" pipe is under the outer steel braiding. Honestly im still kinda dumb founded and i've been "tinkering" with cars for 10+ years. I saved it to hang up on my shed wall with the rest of the FAILED parts. lol
____________________________
97 GS-TALON
|
|
|
|
05-29-2012, 05:12 PM
|
Show Printable Version
Email this Post
#11 (permalink)
|
|
DSMtuners Supporting Vendor

From: aurora, Colorado
Registered: Jul 2006
Reputation:
|
Very common failure.
No more flex section in my car.
____________________________
758/636 Uncorrected with a blow thru GM-MAF
|
|
|
05-31-2012, 06:26 PM
|
Show Printable Version
Email this Post
#12 (permalink)
|
|
Proven Member

From: Omaha, Nebraska
Registered: Nov 2007
|
THis is more common than you might think.. A good friend of mine replaced his low mile BB turbo with the latest version of that model (what's now the 6765) and he was having issues making boost on the first one which is why he replaced it.. Got the new 6765 billet wheel on there and still could barely make 12-15psi out of the car until just a tad before shifting at 8500rpm... He now started wondering what was going on, pulling compression numbers, checking cam timing and so on, it wasn't until he decided to change to a tubular manifold that he brought the DP to me to be modded for the new turbo and awstegate positions and that's when he noticed his had done the same thing and brought it to my attention..
the opening had shrunk down to just over 1.25 inches (roughly measured with a bore caliper/dial)
I garaunteed him this was why he wasn't making boost and wasn't making any good power at the boost he was making.. He was skeptical so i cut the DP apart, made it fit the new manifolds positions and cut the flex off it.. (having no new flex to work with i just tied his cat back up with some SS safety wire and told him to go for a drive) He was instantly boosting beyond 30psi and had to pull over a bunch of times to adjust the boost controller untill he got it settled in the 22psi range (where his wastegate spring is at for a base)
JUst goes to show sometimes it's the simple things you would'nt even consider that needs to be checked on now and again to be sure everything is in good working order..
Do you happen to know what brand that flex piece was?? The one that collapsed on my friends car was a Vibrant piece, I'm just wondering if it's in the build of the flex section or if all of them will do it over time..
We came to conclusion that it was from having the DP hanging from the cat-back connection with it flexing much further than normally required to do it's job, thus causing the steel inside to "bunch up" and restrict the middle in that fashion (we were able to expand it back uot some what and then flexed the pipe repeatedly and duplicated the resulting failure but wasn't sure if it was just becasue that piece had already failed that it re-constricted the way it did)
____________________________
Haltech E6X, Holset H1-3558x, AWD swap
|
|
|
05-31-2012, 06:41 PM
|
Show Printable Version
Email this Post
#13 (permalink)
|
|
Proven Member

From: San Juan, Puerto Rico
Registered: Nov 2007
Reputation:
|
thats a pretty common problem on flex pipes... tip, replace the flex pipe with a Honda spring type pipe..
|
|
|
 |
|
|
» Recent DSM Videos |
|
|
» Online Users: 618 |
| 252 members and 366 guests |
| Most users ever online was 1,704, 03-17-2008 at 09:11 PM. |
|
|
|
|