mikEclipse99
15+ Year Contributor
- 574
- 651
- May 9, 2008
-
Medina,
Ohio
so i bought my 99 gst stock about 6 months ago. i drove it for a month, never got out of temporary tags, then the throttle got stuck at WOT for a good 5 seconds or more. i turned off my car as fast as i could but the turbo timer was still running so i shut that off as well. while the whole thing was happening it was just scary so it took longer to turn it off than it should have. when i turned my car back on it had a knock. that was the last day i drove it for about 3 months. a week later i started pulling out the motor to get it rebuilt. when i took off the TB there was a 2.5" piece of rubber stuck in it. where ever the hell that came from, i dont know. my friends dad owns a machine shop up in cleveland so he was the one going to rebuild it. i got all my parts, spent about $5000 on parts, took it all to the machine shop and he said it would take him about 3-4 weeks to finish. well i got a call about 2 weeks later saying that the pistons werent the right ones. i had bought them from a friends friend. they were supposedly wiseco 9:1 .20 over pistons but i have no clue what they really were. the machine shop also told me that i needed a new crank. so then i bought an eagle 100mm crank and wiseco 9:1 .20 over stroker pistons. a week later the machine shop got them and yet again they were the wrong pistons. extremepsi sent me the wrong ones. so another couple days passed by and the RIGHT pistons arrived at the machine shop. a week or so later he was finally finished with my motor. so in all it took about a month and a half before i got my motor back. we could finally start putting the motor back in. getting it back in wasnt so bad. after we got it in there was an oil leak. i finally located where it was leaking from and it was squirting out of the oil pump gear. the nut wasnt tight enough. so i fixed that then drove it for about a week. the throttle was still sticky like it was previously. i ordered a bbk 62mm TB and a new non cruise throttle cable and now the throttle is perfectly fine. two days ago my check engine light came on and then it started misfiring in cylinder 4. i ran a compression test and cylinders 1, 2 and 3 had around 140psi while cylinder 4 had about 40psi. it turns out the exhaust valve was leaking. i havent removed the head yet but its either bent or burnt. im removing the head tomorrow morning and taking it back to the shop to have them fix it. someday my car will not have any problems oh yeah i forgot...its a DSM. i still love it though. soon as i pay off my debt i can get a new fuel system and a new turbo. it now sits as a 2.3L stroker fully built. ive already dumped $7000 in it and havent even touched the turbo or fuel system...uhhh.