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"Good Ole EVO III 16g days"... Just my thoughts

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I wasn't implying the boost was to high. I'm impressed you got no knock on pump with the boost that high! The SD stuff is actually simple. Plus, there s a good chance you'll make more power (as the dyno will show) by getting rid of the MAF sensor. Nice job overall!

What were your IDC's at on the 850's with 25 - 26 psi and what did you rev the car too?
 
What were your IDC's at on the 850's with 25 - 26 psi and what did you rev the car too?

66.5% on IDC and it looks like he let off at 6800, he's nicer to my car then I am LOL

No I understand about the boost, a lot of people say not to even bother running a 16g at higher boost but overall it hit 26psi and only dropped to 23psi, I know if I ran it to 7500 or beyond it would fall past that but I was still making power to redline.. it might be because I was externally gated

Now i kind of want to switch to SD and see what it does LOL.
 
Something seems off. I'm seeing 25 PSI on my 68HTA V2 faster than you are on your 16G. How bad are the pre-turbo exhaust leaks? Also, what are you using for boost control?

Torque curve comes in late for a 16G car as well.

I'm not terribly familiar with the FP2 cams and how they typically perform. Are these hurting spoolup that badly?

The tune looks good, and airflow is where I'd expect it to be at your boost level. I think you may have a mechanical issue or something at play here that's hindering your results. Thanks for sharing, though. I'm curious to see what the 68 does. Make sure you save this exact tune, and load it up for one of the pulls when you swap turbos and do the future comparison. That will give you a good control variable for the comparison.
 
I need another turbo gonna grab a evo 16g for the rest of the year until I redo everything. One day illgonna grab a other 1gb for my t3 set up holset.
 
Something seems off. I'm seeing 25 PSI on my 68HTA V2 faster than you are on your 16G. How bad are the pre-turbo exhaust leaks? Also, what are you using for boost control?

Installation of the cams had a very noticeable effect on my spoolup - They are installed "straight up" I believe if I degree'd them it would make a huge difference in the behavior of the cams, but as I said before it's just out of my ability to do, I've contemplated going back to stock cams a few times because of this.

Exhaust leaks, I have at least two known leaks at the manifold gasket and a crack split through my manifold to turbo gasket, I meant to do something about them this weekend but I had to get the car on the lift to check out a whining noise - low and behold the yoke for my driveshaft is spitting fluid everywhere, so that take's priority at this point.
With any luck I'll have the parts in by the weekend and I'll do the yoke and swap out the turbo while I'm in there.

I'm disappointed in my spool times, Cory from STM told me that my torque curve basically sucks, and showed me a graph of an evoIII with fp2s putting down 360/360 at the wheels on their dyno, it was an e85 car but the spoolup was much faster then mine, I'm still trying to figure out how to get the video rotated so you guys can see it.
 
Chill out about the wrx thing I'm just more confused now because I've looked at non turbo wrx's for sale at dealerships in my town. http://www.clubwrx.net/forums/everyday-impreza-talk/134303393-non-turbo-wrx.html#/enter

This forum talks about how they shouldn't exist in the USA and I have looked seen them with my own eyes so really I have no freakin clue what to think on that. I thought only the sti was turbo so my bad. (also I'm not a subaru guy) I don't know subarus inside and out because I don't own one.

One thing I do know is I have researched crank walk to the ends of the earth and this made more sense than anything else I've found.

So the other thing, I will bring proof here once I find it again I read about a guy doing blueprints on 7bolt blocks and then doing assembly to find the thrust bearing surface was wiping the oil off the bearing and after much trail and error found that if he machined the thrust surface with a torque plate torqued on with the arp studs that it corrected the issue upon final assembly after- to spell that out basically put torque plate in place of head and throw away head gasket on block, arps torque to spec, machine block, disassembly then whatever desired head gasket and reassembly . He concluded that the actual block strained under the torque of the arp studs something that shouldn't be possible but was- and that was due to a non fixable bad iron structure of the block during casting.

Which some have ventured to guess is why there wasn't a recall issued..

Edit: found it. Thanks
http://www.bcdsm.org/forum/index.php?topic=25724.0

Longer read and in case something gets deleted later:
http://www.dsmtuners.com/threads/update-on-crankwalk-fix.8817/


And because I like to archive everything-
This is for archival purposes in case the other site gets shut down:

Theory of: The cause of crankwalk

Why does crankwalk happen, and what causes it to happy almost solely
on 2G DSM's? To answer this question, you need to look at what makes
the blocks different from eachother, and also look at the actual
metalurgy of the 1G and 2G blocks. From our testing, we have found
that the 1G blocks are actually have a more dense iron content than
the 2G blocks, and are actually stronger. If you notice, on the 1993
and up blocks, they almost seem to have a rib-cage built into them
which is on an engineering level, a very good way to increase
structural integrity. However, something happened in 1995 that
caused Mitsubishi to cheap out on the iron content of the blocks they
were casting. Maybe the R&D of the new car got pricey, and they
needed to cut costs in certain areas or what have you, but those
blocks simply aren't made as strong. The next thing you need to look
at is the thrust area, and that main girdle on the 7 bolt blocks.
Again, from an engineering point of view, a good idea for structural
integrity, and it works great on the 93 and 94 blocks, but again, the
density of the 1995 and up blocks just doesn't quite cut it. This
means you can do one of two things. A. completely change the atomic
composition of the block which would prolly cost you more than your
car did, or B. pick up where Mitsubishi left off, and improve upon
their half-assed design. We chose the latter.

Now, know everyone has been concentrating on oiling, and oil
pressure, and the 2G oil squirters suck, etc. however that idea never
quite held water to me. First off, the oil squirter's main function
is to cool the bottom of the pistons. Secondly, under full throttle,
you are getting upwards of 100psi of oil pressure. 15 pounds of
boost is more than enough air pressure to blow off intercooler pipes
if the clamps are less than perfect, so don't you think 100psi of
liquid pressure would be enough to blow out any bits of grease or
grime in the oil squirters? It doesn't look like a lack of oiling in
my book, from what I have seen on a crankwalked motor. The other
thing I've noticed, is in order to find the cause of crankwalk,
people have dis-assembled blocks, heck, even sliced them in half to
get to the root of the problem. What if the root isn't quite that
deep? What if the cause of crankwalk happens AFTER the short block
begins assembly? If you caught that, read on and I'll elaborate.

Another popular theory of crankwalk is that a heavy pressure plate
causes stress on the crankshaft and literally over time and use will
pull it out of alignment. Those people are actually on the right
track, however something else is failing that is allowing the crank
to be pulled by the pressure plate in the first place. Here comes
our idea. Instead of tearing the block down, and looking at oil
passages, or physically examining the thrust surface, we went the
other way and began assembling, and measuring, and seeing what we
would find. We installed the crank and main girdle, and torqued it
down to factory spec. We then bolted a torque plate on the top of
the block to simulate a cylinder head being bolted down, and we
torqued it to factory spec. What we found ater both had been torqued
was compelling. We measured the thrust area before and after, and
found that it would consistently move .0025-.003" when it had torque
on it! Now, for those who have built and blueprinted an engine
before, .0025-.003" may as well be 2 feet in an area that sees as
much stress and has such a critical job as a thrust bearing. To help
illustrate what is happening here, put your hands together palm to
palm. Now, twist your top hand to the right very slightly and your
bottom hand to the right very slightly. When you "torqued" you
hands, notice they tweaked slightly, and are no longer perfectly
straight. That is what is happening to the 2G block when your
cylinder head is bolted down, and your main girdle is bolted down.
You are causing a condition of pre-mature failure, and things such as
heat, and that heavy pressure plate merely aggravate that existing
problem.

So now we have the root 'cause' of crankwalk, but there's more. This
is going to make sense to those people who have assembled a 4G63
before. When you go to bolt down that main girdle, is there any real
way to line it up perfectly straight? I know I know, the bolt holes
line up, the mains kinda sorta lock into place, yada yada...but are
they going on perfectly straight to the THOUSANDTHS of an inch? If
you can eyeball that, then you are a better man than I. I however,
would put a million dollars on it that there is a measurable
disparity between the tolerances of each main cap, and where it bolts
down. Here's a challenge. Cut the head off a main bolt, and tighten
it down in the hole. Then stick a feeler gauge in there and measure
the clearance between the bolt, and the wall of the bolt hole. Did
you catch it? IF it was going on PERFECTLY sraight, there would be
NO clearance, NO disparity. The bolts would go in much like the
dowels on a flywheel..they would have to be hammered in. Ah ha!
Dowel pins.

A few smart(ly) engineered companies have dowel pinned motors from
the factory; such as Toyota and Nissan. There is a reason for this.
If you are relying on 10 bolts to line up your main girdle, is
essence what you are doing is GUESSING that it's going on straight.
Couple that with your block tweaking and throwing the thrust bearing
off .0025-.003" is like shooting yourself in the foot, and not
learning anything from it. The dowel pins come in to line up that
main girdle PERFECTLY, toleranced to the thousandth of an inch, so
you elliviate any guesswork that may be involved. This is why SOME
motors crankwalk, and SOME do not. Some of the girdles just so
happened to be installed better at the factory, and that is
completely by happenstance and good luck. That's it! However, every
single 2G motor out there does indeed have the capacity to crankwalk,
although some people may never experience it at all.

The Fix

Now that we know what is causing crankwalk, we need to look at how to
fix the problem so it doesn't happen again. First things first, you
must start with a completely flat deck to rule out any possibility of
added 'tweaking' due to an uneven surface (obviously if it goes on un-
evenly, some area will have more pressure applied to them, more
stress, than others.) The block is first cleaned and then decked
true. After that, the main bearing journals are align-honed to
insure we are starting with a perfectly machined bearing surface to
begin with. Then the block needs to be flipped over, and
the 'bottom' end is drilled and machined for dowel pins at 5 points
on the bottom of the block. Matching points are drilled and machined
on the main girdle (obviously, SERIOUSLY close measurements are taken
to ensure everything is perfect..no close, PERFECT.) Just about the
only thing that will withstand than kind of heat is billet steel.
Dowels are formed out of billet steel, and installed into the block.

Obviously at this point, the crank has been inspected, all neccessary
machine work is performed, and it's ready to be installed into the
motor with new main bearings, and new main bolts. The girdle is then
installed on the dowel pins, and hammered down into place. The
dowels are so tight, and fit so well, that you can easily life the
block by it's girdle without any bolts in it. Then the new main
bolts are installed, and torqued to factory spec. The block is
flipped over, and a torque plate is installed to simulate the
cylinder head being bolted down, and then torqued to factory head
bolt specs. The thrust area is measured with everything torqued,
tolerance disparity is recorded, and the block is disassembled. The
crank and bearings are removed, and the process or torqing the torque
plate and main girdle is repeated minus the crank and bearings, and
then the thrust area is re-machined with everything torqued down to
be 100% perfect again. Not close, perfect. The bearings, crank, etc
are all re-installed, and re-measured. The thrust bearing now did
NOT move. Dowel-pinning the main girdle ensured that it went on
perfectly straight every single time which eliminates guesswork and
allows for precise machining.

Regards,
I was having thoughts of rebuilding my engine myself.until I read this..
I'm a have to take it to a trusted shop to get it perfect...
 
I went to an HX40 in 2015. Car was much faster but not as fun. I put an e3 16g back on it now.

Best time 11.6@119mph full weight, 205 junk walmart douglas all season tires. Stock trans stock bottom end. Hell at that time too my clutch was slipping. Fully expect an 11.2-11.4 if I ever go back to the track on it.
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More than enough to have fun and stupid simple/cheap/reliable.
 
Best time 11.6@119mph full weight, 205 junk walmart douglas all season tires. Stock trans stock bottom end. Hell at that time too my clutch was slipping. Fully expect an 11.2-11.4 if I ever go back to the track on it.

Do you have a log of that pass? I'm very impressed by that!

I should of taken my car to the track but I'm not confident enough in myself to launch the car.. LOL
 
Psh, the last time I went to a track I launched my camaro.. stalled it to 3k, light turns green and BANG.. roll forward about 6 inches. First time that car ever got full traction off the line and the rear end grenaded. Since then I'm a bit shy about dragstrips. I have no doubt a lot of you guys have simliar/worse stories, but I was young and it left a bad taste in my mouth, haven't raced since then.

I'll get out there soon enough, Let me get the 68hta dialed in and I'll go make some passes, but probably no launching LOL
 
"Good Ole Evo III 16g days"...

I'm still on a 14b! Great thread through...reinforces why I'm building my car slowly. Well, that and the fact that I blew the 7-bolt up in 2004, only finally replaced it with a 2.3l 6-bolt in 2013 and have only seen the car for about 2-weeks a year since, so it's kind of stuck in a time warp.:p
 
Sorry for the random post, I'm currently in the process of upgrading from an e85 evo 3 16g setup to an fp red. I've ran the turbo for 3 years now and loved every minute of it. I've surprised so many people on the streets with this "small" turbo LOL. It really Is a great turbo for 2.0 liter motor. I ran a best of 13.2 at 105 at altitude at bandimere speedway in Colorado which is nice for such high altitude, not to mention its a stock 130k mile 26 year old motor that still hauls ass
 
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