kelvinb
15+ Year Contributor
- 726
- 3
- May 7, 2004
-
Lincoln,
Nebraska
k im hitting about 10psi at most (wastegate)
2g elbow
custom uicp
supra smic
dejon tool licp
dejon tool turbo outlet pipe thingy
stock 14b
stock 450s
3in turboback mandrel bent no cat
wal255
rewired
aeromotive afpr - 38psi
fidanza flywheel
exedy stage 2 clutch
KN filter
hacked maf
modded 1g bov (not crushed-the extra nipple)
mix of 4g of 91 and 4g of 100oct
fuel trims were like 139low 103mid 105high
ok i have one small boost leak, as in holding 20psi for about 3-4 minutes but does drop. the leak is from the turbo, not the intake or outlet pipe, its from where it connects to the catridge. anyways the most recent mods are the aeromotive afpr and 255. before i put in the 255 i was getting af of about 12.5-13 according to wideband. after 255 with stock fpr i was getting around 9:1 af, so i got the aeromotive afpr. after installing it i was not able to use the wb since the threads were f'd up by a friend using it. anyways i did some logs with MMCd 1.8 and basically whats happening is its backfiring like a mother####, only at high rpms. base pressure is set at 38psi, boost is not passing 10psi, im doing 2nd and 3rd gear pulls and im confused. someone helpz0r
2nd gear
timing 02 tps rpm knock p/w dono
25° 0.78V 100.0% 3313 0 11.78ms 208
23° 0.84V 100.0% 3563 0 15.87ms 255
16° 0.86V 100.0% 3938 0 17.92ms 255
18° 0.86V 100.0% 4219 0 18.94ms 255
18° 0.86V 100.0% 4563 0 20.48ms 255
18° 0.88V 100.0% 4781 0 20.99ms 255
19° 0.84V 100.0% 5031 0 20.48ms 255
20° 0.86V 100.0% 5250 0 20.48ms 255
18° 0.86V 100.0% 5531 1 d/c 96% 20.99ms 255
21° 0.88V 100.0% 5719 0 d/c 96% 20.22ms 255
19° 0.78V 100.0% 5813 5 d/c 93% 19.46ms 255
21° 0.88V 100.0% 5906 5 19.46ms 255
16° 0.64V 100.0% 7969 4 8.70ms 255
17° 0.84V 100.0% 6031 4 d/c 0% 0.00ms 246
17° 0.80V 100.0% 7969 10d/c117%17.66ms 255
one thing for sure is im not hitting 8k rpm. its backfiring like a mother after 5800rpm and i dont know why. again this is only 10psi.
3rd gear same deal
25° 0.49V 89.4% 3031 1 9.98ms 190
22° 0.80V 92.2% 3125 0 12.80ms 220
19° 0.86V 92.5% 3281 0 16.13ms 255
15° 0.86V 92.9% 3375 0 17.66ms 255
15° 0.86V 93.3% 3563 0 16.90ms 255
16° 0.86V 93.3% 3750 0 16.64ms 255
17° 0.86V 93.3% 3875 0 16.64ms 255
18° 0.86V 93.7% 4031 0 17.15ms 255
18° 0.86V 93.7% 4188 0 17.15ms 255
18° 0.86V 94.1% 4344 0 17.92ms 255
18° 0.88V 94.1% 4406 0 19.20ms 255
18° 0.88V 94.5% 4594 0 19.97ms 255
18° 0.88V 94.9% 4625 0 20.99ms 255
18° 0.88V 94.9% 4875 0 21.50ms 255
19° 0.88V 95.3% 5031 0 21.50ms 255
19° 0.88V 95.7% 5094 0 21.50ms 255
20° 0.86V 96.1% 5156 0 21.76ms 255
20° 0.82V 97.3% 5219 0 21.50ms 255
21° 0.86V 97.6% 5438 0 21.25ms 255
22° 0.86V 98.0% 5469 0 d/c 96% 21.25ms 255
21° 0.88V 98.0% 5563 0 21.25ms 255
18° 0.86V 98.4% 5656 0 18.43ms 255
23° 0.84V 98.4% 5813 0 20.22ms 255
23° 0.86V 98.8% 5719 0 d/c 89% 18.69ms 255
24° 0.86V 98.8% 5906 0 19.20ms 255
24° 0.74V 99.2% 7969 11d/c121%18.43ms 255
20° 0.64V 99.6% 5906 11 19.20ms 255
14° 0.82V 99.6% 6125 10d/c 97% 19.20ms 255
2g elbow
custom uicp
supra smic
dejon tool licp
dejon tool turbo outlet pipe thingy
stock 14b
stock 450s
3in turboback mandrel bent no cat
wal255
rewired
aeromotive afpr - 38psi
fidanza flywheel
exedy stage 2 clutch
KN filter
hacked maf
modded 1g bov (not crushed-the extra nipple)
mix of 4g of 91 and 4g of 100oct
fuel trims were like 139low 103mid 105high
ok i have one small boost leak, as in holding 20psi for about 3-4 minutes but does drop. the leak is from the turbo, not the intake or outlet pipe, its from where it connects to the catridge. anyways the most recent mods are the aeromotive afpr and 255. before i put in the 255 i was getting af of about 12.5-13 according to wideband. after 255 with stock fpr i was getting around 9:1 af, so i got the aeromotive afpr. after installing it i was not able to use the wb since the threads were f'd up by a friend using it. anyways i did some logs with MMCd 1.8 and basically whats happening is its backfiring like a mother####, only at high rpms. base pressure is set at 38psi, boost is not passing 10psi, im doing 2nd and 3rd gear pulls and im confused. someone helpz0r
2nd gear
timing 02 tps rpm knock p/w dono
25° 0.78V 100.0% 3313 0 11.78ms 208
23° 0.84V 100.0% 3563 0 15.87ms 255
16° 0.86V 100.0% 3938 0 17.92ms 255
18° 0.86V 100.0% 4219 0 18.94ms 255
18° 0.86V 100.0% 4563 0 20.48ms 255
18° 0.88V 100.0% 4781 0 20.99ms 255
19° 0.84V 100.0% 5031 0 20.48ms 255
20° 0.86V 100.0% 5250 0 20.48ms 255
18° 0.86V 100.0% 5531 1 d/c 96% 20.99ms 255
21° 0.88V 100.0% 5719 0 d/c 96% 20.22ms 255
19° 0.78V 100.0% 5813 5 d/c 93% 19.46ms 255
21° 0.88V 100.0% 5906 5 19.46ms 255
16° 0.64V 100.0% 7969 4 8.70ms 255
17° 0.84V 100.0% 6031 4 d/c 0% 0.00ms 246
17° 0.80V 100.0% 7969 10d/c117%17.66ms 255
one thing for sure is im not hitting 8k rpm. its backfiring like a mother after 5800rpm and i dont know why. again this is only 10psi.
3rd gear same deal
25° 0.49V 89.4% 3031 1 9.98ms 190
22° 0.80V 92.2% 3125 0 12.80ms 220
19° 0.86V 92.5% 3281 0 16.13ms 255
15° 0.86V 92.9% 3375 0 17.66ms 255
15° 0.86V 93.3% 3563 0 16.90ms 255
16° 0.86V 93.3% 3750 0 16.64ms 255
17° 0.86V 93.3% 3875 0 16.64ms 255
18° 0.86V 93.7% 4031 0 17.15ms 255
18° 0.86V 93.7% 4188 0 17.15ms 255
18° 0.86V 94.1% 4344 0 17.92ms 255
18° 0.88V 94.1% 4406 0 19.20ms 255
18° 0.88V 94.5% 4594 0 19.97ms 255
18° 0.88V 94.9% 4625 0 20.99ms 255
18° 0.88V 94.9% 4875 0 21.50ms 255
19° 0.88V 95.3% 5031 0 21.50ms 255
19° 0.88V 95.7% 5094 0 21.50ms 255
20° 0.86V 96.1% 5156 0 21.76ms 255
20° 0.82V 97.3% 5219 0 21.50ms 255
21° 0.86V 97.6% 5438 0 21.25ms 255
22° 0.86V 98.0% 5469 0 d/c 96% 21.25ms 255
21° 0.88V 98.0% 5563 0 21.25ms 255
18° 0.86V 98.4% 5656 0 18.43ms 255
23° 0.84V 98.4% 5813 0 20.22ms 255
23° 0.86V 98.8% 5719 0 d/c 89% 18.69ms 255
24° 0.86V 98.8% 5906 0 19.20ms 255
24° 0.74V 99.2% 7969 11d/c121%18.43ms 255
20° 0.64V 99.6% 5906 11 19.20ms 255
14° 0.82V 99.6% 6125 10d/c 97% 19.20ms 255
. i checked the resistance from my power wire to my relay rewired pump) and its .3-.4 resistance in the line, so power is ok. also checked the power to the relay, its like 12-13v i forget. so i dont think the pump oring or the wiring is the problem, unless .3-.4 is bad for resistance through line. im going to regap my plugs now and i dono whats next