Blog Title: I just wanna be mobile again. Fast would be nice.
Well I picked my 95 GSX up in August of 2009. She had a few issues like boost leaks, the LOOK at ME paint job, ricer body kit and side mirrors I could see out of.
Within a week of purchase, I took her up to Mach V since i lived only 20 minutes away. Quick once over discovered that my radiator was leaking from the top plastic end tank, It had some hairline cracks that were spiderwebbing out. SO, I scheduled some shop time for basic maintenance, install of new mishimoto radiator, and compression and leakdown testing. Day before i had shop time scheduled, Naomi stalls out on me, in DC rush hour traffic, on a 4 lane bridge. Timing marks were still correct, she still had fuel, but no spark. Not something I could diagnose at the time, so I towed her to Mach V.
Turns out Naomi had shredded the balance shaft belt, which ate the crank position sensor, so there was my no spark issue.
Well after the shop changed all her fluids, installed her new radiator, new kevlar timing and balance shaft belts, new shifter bushings, new boost gauge she was back on the road.
Then a few weeks later, coming home from skyline drive, The DSM dropped a valve, and grenaded the lower end.... FANTASTIC!
So it took six months, but i rebuilt the motor while block was still in the chassis. PAIN IN THE REAR, will NEVER do it that way again. But she was running fantastically. All the way until she turned over 320 miles, and a rod SHEARED doing 55 in 5th gear, had been cruising for 2 minutes. The rods were shotpeened and magnafluxed when I had new pistons pressed onto them.


So, She sat in Vienna, Va for about 18 months.. Until I moved back home to Jacksonville, Fl and towed her behind me.


Within a week of purchase, I took her up to Mach V since i lived only 20 minutes away. Quick once over discovered that my radiator was leaking from the top plastic end tank, It had some hairline cracks that were spiderwebbing out. SO, I scheduled some shop time for basic maintenance, install of new mishimoto radiator, and compression and leakdown testing. Day before i had shop time scheduled, Naomi stalls out on me, in DC rush hour traffic, on a 4 lane bridge. Timing marks were still correct, she still had fuel, but no spark. Not something I could diagnose at the time, so I towed her to Mach V.
Turns out Naomi had shredded the balance shaft belt, which ate the crank position sensor, so there was my no spark issue.
Well after the shop changed all her fluids, installed her new radiator, new kevlar timing and balance shaft belts, new shifter bushings, new boost gauge she was back on the road.

Then a few weeks later, coming home from skyline drive, The DSM dropped a valve, and grenaded the lower end.... FANTASTIC!

So it took six months, but i rebuilt the motor while block was still in the chassis. PAIN IN THE REAR, will NEVER do it that way again. But she was running fantastically. All the way until she turned over 320 miles, and a rod SHEARED doing 55 in 5th gear, had been cruising for 2 minutes. The rods were shotpeened and magnafluxed when I had new pistons pressed onto them.



So, She sat in Vienna, Va for about 18 months.. Until I moved back home to Jacksonville, Fl and towed her behind me.



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Posted in DSM Project Car/Build Updates
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